Overview
Statistic | Value |
---|---|
Propellant Weight | 13.5 lbs |
Impulse | Unknown |
Classification | Unknown |
Delivered isp | Unknown |
Video
Failure Analysis
After extensive analysis it was determined that the thermal liner was cut ~ .125in short. This allowed the closure rings to bottom out without sufficiently compressing the o-rings. The lack of sealing lead to gas blowby and a thermal meltdown of the forward closure. The forward insulating disk was also identified as a risk due to it's one-off construction method, and low quality material selection. (Don't dremel flight critical components from fire resistant bathroom tiles)